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Failure analysis method and case of pipe sleeve

Recently contacted with a batch of long cylinder workpieces (see Fig. 1). During the acceptance of finished products, cracks were found on the surface of inner holes of four products. One of the most typical samples was cut and analyzed, as shown in Fig. 2 and Fig. 3.

Long barrel workpiece

Fig.1 Long barrel workpiece

Sectioning

Figure.2 Sectioning

Cracks and sampling positions found by MT after sectioning

Fig.3 Cracks and sampling positions found by MT after sectioning

Physical and chemical test and results

Chemical composition

The chemical composition of H1 sample was detected by direct reading spectrometer, and the results are shown in Table 1.

Table.1 results of spectral chemical composition analysis of H1 sample (mass fraction) (%)

Element

C

Si

Mn

P

S

Cr

Mo

Ni

Cu

Standard

EN10083-3

0.38~0.45

≤0.40

0.60~0.90

≤0.025

≤0.025

0.90~1.20

0.15~0.30

Actual measurement

0.40

0.22

0.74

0.010

1.14

0.225

0.13

0.03

Hardness

Use Rockwell hardness tester to test the hardness value of H1 and B1 samples in the direction of wall thickness, and the results are shown in Table 2.

Table.2 Hardness distribution in the direction of wall thickness of H1 and B1 samples (HRC)

Hardness

Sample

1

2

3

4

5

Average value

H1

29.0

25.8

26.3

27.7

28.0

27.4

B1

30.3

30.6

28.7

29.1

23.6

28.5

Microstructure

Grind and polish H1 specimen along n-PLANE and k-plane (see Fig. 4) (n-PLANE is the surface of inner hole, k-plane is the grinding and polishing surface along the direction of wall thickness), and observe in turn with microscope. The crack morphology of n-PLANE after polishing is as shown in Figure 5. Then, the polishing surface was eroded with 4% nitric acid alcohol solution, and the microstructure near the crack was observed, as shown in Fig. 6. The crack morphology and microstructure after erosion of surface k after polishing are shown in Fig. 7.

Grinding and polishing of H1 sample

Figure.4 Grinding and polishing of H1 sample

Crack morphology (50x) after polishing the inner hole surface of H1 sample

Fig.5 Crack morphology (50x) after polishing the inner hole surface of H1 sample

Microstructure near inner hole surface crack of H1 sample (500X)

Fig.6 Microstructure near inner hole surface crack of H1 sample (500X)

K-plane crack and microstructure of H1 specimen

Figure.7 K-plane crack and microstructure of H1 specimen

The B1 specimen (see Figure 8) was polished and eroded along the n-PLANE and the k-plane respectively (n is the inner hole surface, K is the polishing surface along the wall thickness direction), and the crack morphology and microstructure nearby were observed under the microscope.

Grinding and polishing of B1 specimen along n-PLANE and k-plane respectively

Fig.8 Grinding and polishing of B1 specimen along n-PLANE and k-plane respectively

There are many cracks on the inner hole surface of B1 sample. Under the microscope, its morphology is shown in Figure 9. Then, 4% nitric acid alcohol was used for erosion, and the microstructure near the surface crack of the inner hole was observed, as shown in Figure 10.

N-PLANE-crack-morphology-of-B1-sample

Figure.9 N-PLANE crack morphology of B1 sample (50x)

Microstructure near n-PLANE crack of B1 sample

Fig.10 Microstructure near n-PLANE crack of B1 sample

After polishing in the direction of wall thickness of B1 sample, the crack morphology is as shown in Figure 11.

N-PLANE crack morphology of B1 sample

Figure.11 N-PLANE crack morphology of B1 sample

After etching the k-plane with 4% nitric acid alcohol solution, observe the microstructure near the crack, as shown in FIG. 12.

Microstructure near k-plane crack of B1 sample

Fig.12 Microstructure near k-plane crack of B1 sample

Result analysis

From the above analysis results, it can be seen that the chemical composition of the raw material used for this part meets the requirements of 42CrMo4 in en 10083-3, and no element exceeding the standard is found. According to the hardness test results of the cut-off test block, there is no obvious gradient change in the hardness of the pipe sleeve along the thickness direction, which indicates that the workpiece has been hardened thoroughly and tempered fully during quenching.

According to the actual heat treatment process of the pipe sleeve, the actual heat treatment process curve is shown in Figure 13, and no abnormality is found in the production process.

Quenching and tempering curve of sleeve

Fig.13 Quenching and tempering curve of pipe sleeve

From the crack morphology observed after grinding, the crack tip on the inner hole surface and wall thickness direction of sample H1 and sample B1 is relatively sharp, and its propagation path is transgranular, which is a typical quenching crack. According to the microstructure after erosion, the microstructures near the cracks of the two samples are tempered sorbite, no massive ferrite and long strip ferrite are found, and no obvious oxide decarburization layer is found on both sides of the cracks. This shows that the cracks are formed in the process of heat treatment.

In fact, for the finished long tube parts, the wall thickness is 40mm (thin wall end) and 52mm (thick wall end), respectively. In general, the inner hole is relatively long, the inner diameter is small and the wall thickness belongs to 42CrMo4 steel, which can be fully quenched, and the structure stress is relatively large during quenching. At the same time, for the deep hole parts with small inner diameter, because the cooling speed of the inner surface is much smaller than that of the outer surface and the effect of residual thermal stress is small, the tensile stress on the inner surface is larger than that on the outer surface, and it is easy to form longitudinal cracks on the inner surface, or even multiple parallel cracks (see Figure 14).

Distribution and crack of quenching residual stress of deep hole parts

Figure.14 Distribution and crack of quenching residual stress of deep hole parts

Conclusion and preventive measures

  1. (1) Through the body sampling analysis, it can be seen that the pipe sleeve crack belongs to a typical quenching crack, which is caused by the excessive internal stress of the workpiece during quenching, especially the excessive tensile stress on the surface of the inner hole.

  2. (2) In order to avoid this kind of cracks, measures can be taken to reduce quenching temperature, increase the speed and efficiency of quenching medium flowing along the inner hole, and increase the final cooling temperature, so as to reduce quenching stress and avoid workpiece cracking.

Source: China Pipe Sleeve Manufacturer – wilsonpipeline Pipe Industry Co., Limited (www.wilsonpipeline.com)

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